KARST AQUIFER TEST REPORTS
LEMON LANE LANDFILL
OCTOBER-NOVEMBER 2001
Released: March 13, 2002
Purpose
1.0 Introduction
A series of aquifer tests were performed in October and November 2001 at the Lemon Lane
Landfill and surrounding area. The general purpose of the tests was to further evaluate the
potential karst pathways from the site to the Illinois Central Spring system.
Four tests were conducted. The testing period began on October 31, 2001 and was
completed on November 23, 2001. During this time there were no major storm events.
Figure 1 is a plot of measurable rain fall and mean temperatures in the Bloomington area
during the test period. The test period was bounded by significant rain on October 24, 2001
and November 25, 2001. Temperatures were typically mild for November.
The first test was a dye injection. The dye injection occurred on October 31, 2001 with
follow up sampling conducted at various locations from two days to several weeks. On
November 7, 2001 a pump test was conducted at borehole MW21. This well is located on
the east side of the landfill. This test lasted until the afternoon of November 9, 2001. On
November 13, 2001, a second pump test was conducted at borehole MW16. This test was
concluded on November 19, 2001. Finally, an injection test to Sargent's Pond was
conducted on November 20, 2001. Monitoring for the injection test ceased on November 23,
2001.
The following sections describe the test results.
2.0 Dye Testing
2.1 Introduction
Three different dyes were injected on October 31, 2001:
Eosine was injected at NN700 at 10:15 to 10:27
Phloxine was injected at SP 1 at 11: 15 to 11:26
Fluorescein was injected at LF6-8 at 11:50 to 11:51
For each of the injections, 300 grams of dye were mixed with a gallon of water. For wells
NN700 and SP 1, this water was then injected using a peristaltic pump with discharge tubing
placed at the 795 elevation. For LF6-8 the dye/water mix was just poured down the well
casing. All initial dye injections were followed by 110 gallons of flushing water. The
bottom of the LF6-8 casing is sumped in approximately 3 feet of clay, which holds about 8
gallons. So residual dye remained in the hole after initial flushing. In addition to the
injections on October 31, 2001, water was also flushed into LF6 on two additional occasions
and into NN700 and SP1 on one separate occasion. These additional flushes of water were
done in concert with pump test conducted in November 2001, and were intended to flush
residual dye out of the well bore. The water flush results will be discussed separately in the
report on the pump tests.
Wells around Lemon Lane and four springs (Illinois Central, Quarry B., Slaughterhouse and
IC Weir) were monitored for the dyes injected on October 31 by sampling at various
periodicity. The test plan, Attachment 1, was essentially completed.
The goals of the dye test were basically threefold. First, to determine if any of the wells
surrounding the site were on or near a major conduit which would integrate all three dyes
into one flow path towards the IC Spring. Second, to determine travel times from various
areas of the site to the IC Spring. Third, to determine if Quarry B would receive dye while
flow was stopped to the swallow hole. The Quarry B goal was done in concert with the EPA
who is trying to determine if underflow occurs between IC and Quarry B Springs.
All the dye results have been summarized on tables by sampling locations. These tables are
presented as Attachment 2. The attachment includes dye sampling conducted in concert with
the pump testing performed at later dates and also discussed in Section 3. The initial dye
results from the October 31 injections will be discussed on a dye by dye basis in this report.
First, background results are discussed in Section 2.1.1.
2.1. Background Fluorescence Samples
Attachment 2 includes the samples, locations and results taken for background fluorescence
prior to the dye injection. Not every station sampled had background samples taken, as some
stations, e.g. Valhalla "A" wells, were added to the sampling plan during the test.
There are several sources for background fluorescence. Natural occurring organic
compounds such as certain algae, chlorophylls, and manure leachates can fluoresce in the
blue-green range near Fluorescein. Anthropogenic sources include radiator coolant
(Fluorescein), brake and transmission fluid (Rhodamine which would be similar to Phoxine
B), and septic discharge containing laundry detergents (blue-green opticalbrighteners) and
shampoos (green and red dyes). However, previous dye trace injections at Lemon Lane are
by far the greatest source of background fluorescence. These include.
- 1989 Direct Yellow in wells MWls and MWld
- 1989 Optical Brightener in MW7
- 1989 Fluorescein in MW10
- 1990 Rhodamine WT in MW10, MWls, MW7
- 1992 Fluorescein, Rhodamine WT, Eosine, Optical Brighteners, and Direct Yellow in
five sinkholes around Lemon Lane
- 1996 Fluorescein in swallow-holes in southwest corner of landfill
- 1996 Rhodamine WT in North Sink (900' north of
the site)
It has been discovered recently that Rhodamine WT, once in the environment, breaks down
into compounds that fluoresce anywhere from 520 nanometers to 578 nanometers.
Illinois Central Spring had background fluorescence for both Fluorescein and Rhodamine
WT. If the samples between injection and first detection on the breakthrough curve are
counted as background, then background Fluorescein ranged from 0.11 to 0.13 ppb.
Quarry B spring also had minor amounts (less than 0.1 ppb) of Fluorescein in the background
samples as did the Swallow-hole seep.
Minor amounts of Fluorescein were seen in 00-370 and 00-300. A Phloxine-like
fluorescence was seen in 00-587 on a lOxlO scan, but does not appear on any of the 5x5
scans during the test. NN-625 has a small amount of degraded Rhodamine WT and a 0.7 ppb
background Fluorescein, but neither one shows up again during the test. An Eosine-like
fluorescence appears in a MW6 background at lOx10 scan, but does not reappear in any of
the 5x5 scans during the test.
MW15 was the only Lemon Lane well to show Fluorescein background, besides
MW1O. No Fluorescein appeared in the well during the test. MW10 had Fluorescein
injected in it in 1989 and showed a 37 ppb residual level in its background sample.
MW1O also had high amounts of Rhodamine WT residual. Because of these residuals,
MW10 was not sampled during the test. MW16, 18, and 19 had background samples clear of
fluorescence. The other wells near MW10 (MW20, MW21, MW4i, MW4s, and MW17)
showed varying amounts of degraded Rhodamine WT, in background, as well as during the
test as did MW2. These high degraded Rhodamine WT residuals were probably a
contributing factor to the lack of detection of Phloxine B during the test. These high
backgrounds also make any isolated dye detection in the absence of a breakthrough curve
during the test suspect.
2.2 Fluorescein
2.2.1 Well Samples
By far the most unambiguous dye detections at both wells around the site and IC spring were
for the Fluorescein injected at LF6-8. Fluorescein was detected at wells 00370, NN300,
NN300A, 00300A, 00300 and 4S. Table 1 summarizes the detection of Fluorescein at the wells around Lemon Lane. Figure 2 shows the well locations and those that received hits of
Fluorescein.
It should be understood that the method of sampling wells might lead to some confusion
about the results. All of the wells but one were generally sampled by hand using a dedicated
bailer in each well. The bailer would be pulled up and emptied into a sample jar. Then the
bailer would be dropped back down the well and suspended until the next sample time.
Since bailers fill when dropped down a well bore, the sample time listed for any well sample
sampled in this manner can be misleading. The samplers were generally agitated up and
down in the well bore before pulling the bailer up at the sample time. This would mix the
water in the bailer. So it would be most correct to consider any sample taken this way to be a
mixture of water that was in the hole at the time it was placed down the hole (the previous
sample time) and the present sample time water. In other words a sample listed as taken at
12:00 may actually be a mix of conditions at the well the previous sampling time and the
current sample time.
Another important fact about this method is that the well is not purged at all with this
method. This implies that the well would have to be very close to or on a conduit to receive
a significant hit of dye. The exception to this sampling scheme was MW21. This well was
purged and sampled with a submersible pump each time.
These Fluorescein results are significant in that Viacom had always assumed that the water in
the epikarst at Lemon Lane would flow down dip (to the southwest), then descend to the
phreatic zone, and flow laterally to the spring in a conduit that would generally following the
non-storm potentiometric surface. However, this hypothesis was based on examples given
by Palmer1 (1999) for other karst aquifers. These dye results do prove that at least some of
the water/dye mix injected at LF6-8 (an epikarst well) did flow to the southwest into Valhalla
cemetery. They also suggest that this flow occurred in the epikarst to a point beyond NN300,
then some of the dye descended to the phreatic zone and flowed back toward the site (this
would match the direction of the low flow potentiometric surface in the area of the site).
This would explain the appearance of dye in well 00370 before well NN300.
Note that wells NN300A and 00300A are shallow wells that do not extend all the way to the
795-800 feet amsl horizon while most of the other wells (such as 00370 and NN300) do.
These shallow wells were not sampled at the same frequency as the deeper wells, nor were
background samples taken. The first samples taken from these wells were the November 1
11:30 samples. The dye was already present in high concentrations, so minimum travel times
cannot be ascertained. These shallow wells have by far the highest concentrations of
Fluorescein found in any well or spring sample, which implies they are nearest a primary
pathway. It also implies the primary pathway is above the 795-800 horizon.
Well 4S is the only non-Valhalla well which received an apparent large hit of Fluorescein.
Since only one sample at this location was positive for the dye, there is some question about
the validity of this result. It should be noted that 22 kilograms of Fluorescein was injected in
well MW10 in 1989 and 37 ppb residual concentration was noted in that well in the
background sample. All other locations that tested positive for Fluorescein had more than
one sample from that location containing the dye. The timing of the sample also causes some
concern for its validity. The sample on Table 1 from well 4S that is listed as collected at
October 3 l at 17:35 may in fact have contained mostly water that was in the well column at
13:40 on October 31 when the bailer was last dropped down the well column. Since well
LF6 was injected at 12:00 on October 31, it seems unlikely that Fluorescein would have
made it to well 4S within 1 hour and 40 minutes. Therefore, the detection of Fluorescein in
this well is more questionable than the other wells.
On the other hand, Mike McCann took this sample and recalls this particular sample being
tinted green in the bailer. This would indicate that it is not a lab analysis error, or a labeling
problem. Another indication that this is a real detection is the detection of Fluorescein in
MW21 once pumping of this well started on November 7, 2001. Low levels of Fluorescein
show up in this well within a half hour of starting the pump. This would indicate some of the
dye residual was near the well. Although note that this residual could be from the 1989
injection at MW 10. Well 21 and 4S are within 10 feet of each other. If this is a valid
detection of the Fluorescein injected in LF6-8 in well 4S, it would indicate that a very fast
connection (a conduit) exist between LF6-8 and 4S.
2.2.9 Spring Samples
Although small background levels were detected in the Swallow-hole Seep and at Quarry B.
a distinct breakthrough curved for Fluorescein was seen only at IC Spring. See Figure 3.
This shows the Fluorescein concentrations over time at IC Spring for the dye test period.
Note there is a "saw toothed" peak period between November 1 14:00 end November 2 14:00
followed by a single large maximum at November 2 20:00. This would indicate that there
are at least two flow paths from the injection point to the spring. The first arrival at IC spring
occurred at 09:00 on November 1, 2001. This is a travel time of 21 hours. The second flow
path has a first arrival time of approximately 52 hours after injection (this arrival time is most
likely skewed later than the actual time since the first dye arrival is so significant) and there
is peak overlap.
To further evaluate the dye recovery at the IC Spring, a computer program developed by
EPA for quantitative dye recovery analysis in karst terrane was run on these results. Table 2
summarizes the pertinent features of this dye injection from the computer model. As can be
seen from the table, there is much more dye mass calculated to be recovered at the spring
than was actually injected during the test. Usually, much less dye is recovered than was
actually injected due to sorption and dead space/dispersion losses along the aquifer.
This indicates a significant error in one or more of the parameters used to calculate the mass
recovery (water flow and dye concentrations at the spring). Since water flow is calculated
from sump fill rates (which should be accurate with design and/or as-built drawings), and
seems to not be significantly off, based on time of year and proximity of rain events, the
evidence points to dye concentrations as the most likely error. Unless this is resolved, all
users of the data should be cautioned that the dye concentration data should be considered
semi-quantitative. Some likely causes of quantitation error include:
- The unknown impact of a mixture of dyes on machine calibration. Note that the
calibration curves were run on single dye mixtures. While in reality three dyes were
injected and all three could have arrived at the spring at similar times resulting in a 3
component mix. The impact on quantitation for one dye of a 3 component mix is not
known.
- The calibrations were done with distilled water. Some unknown component in the
actual spring water could be causing an error. Background samples at the spring did
indicate some interfering amount of Fluorescein at levels from 2-24 ppb prior to
injection. This high background will cause some error, but not the magnitude of error
apparent in this data.
- Most of the 3x3 scans conducted on samples from
IC Spring had results which were above the calibrated range of the
instrument. For example, the highest 3x3 calibration standard run had an
intensity of 160 IU. Out of 40 3x3 scans run, only 3 had an intensity
lower than 160. Typically, samples with an intensity higher than the
highest calibration standard should be diluted to an intensity value
below the highest calibration standard to ensure accurate results. By
contrast, only 1 out of almost 100 SxS scans were reported at an
intensity above the calibrated range. This implies the SxS scan data is
more accurate then the 3x3 data. The 3x3 scans were used almost
exclusively during the heaviest dye arrival period at the spring. A
large error in those samples could cause a large overall error in
recovered dye mass.
The first arrival time of 21 hours after injection compares to a PCB travel time of 14 hours at
the actual flow rates experience during the test period. This means that the PCB pulse during
a small storm event would be expected to beat the dye to the spring by 7 hours. This
difference could be due to some allowance for travel in the epikarst. It is not known if the
PCB travel time correlation with flow developed from storm data is applicable to the dye
travel time found during this non-storm condition. If it is directly applicable, this travel time
would indicate that the PCBs which first arrive at the spring during storms take a shorter
route than the dye injected at LF6-8. A dye injection in LF6-8 concurrent with a storm event
would clarify this.
There was one very low level Fluorescein detection at Quarry B spring on November 1 at
01:00. The level detected was lower then some background samples at the spring and also
the detection occurred prior to detections at IC Spring. These two facts decrease the
probability that this is a valid detection of the Fluorescein injected during this dye test.
Fluorescein was not detected at Slaughterhouse Spring. This spring was sampled for almost
two days after injection.
2.3 Eosine Detections
2.3.1 Wells
Eosine was detected in the following wells around Lemon Lane:
MW 15,16, 18,19,20,21 and MW2 on the east side of Lemon Lane and NN 625, 00587,
00370, NN300 and 00387 in Valhalla. These results are summarized in Table 3. All of
these detections are at much lower levels than found for the Fluorescein.
By far the highest level detected on the east side of Lemon Lane was found in MW20 and
MW 21 and in Valhalla in 00587. The other levels of detection in the east side wells are
low. This causes some question about the validity of the detections on the east side in wells
other than 21 and 20. However. the detections on the east side of the landfill make sense
with the injection time. There was also no cosine detected in any pre-injection background
samples for these wells. Therefore in the aggregate, we should assume these are valid
detections.
The first detection of the cosine was in 00370 on October 31 at 14:26. This was followed
by detections at MW16 (17:10), MW21 (19:00), MW2 (20:53), MW18+19 (21:50) and
MW20 on November 1 at 01:28. This would indicate that water flowing near NN700
generally flows in an eastnortheast direction. With generally the higher levels on the east
side found in MW21/20, this indicates that these wells are nearer a collection point for this
water. Figure 4 depicts an interpretation of these results.
2.3.2 Springs
Eosine was not detected at any of the springs after the initial injection. The two most likely
explanations for this are that either the cosine arrival at the IC Spring was masked by the
much larger Fluorescein detections at IC Spring (implying that its travel time is slower) or
that the cosine was diluted beyond detection limits. IC Spring was intensely monitored for
an extended period of time after injection. Slaughterhouse Spring was monitored
sporadically for up to 1 week after injection.
2.4 Phloxine
Phloxine was not detected unambiguously in any well or spring until pumping of MW2 1
began on November 7, 2001. There are several possible reasons for this. First, it is not
known if enough phloxine was injected. Its sorption properties may be such that it requires a
much more massive injection than we performed to be detectable in our system. Second, it
may have been at the IC spring at the same time the more massive amounts of Fluorescein
were present and the Fluorescein may have masked the phloxine. Third, the dye could have
gone to an un-monitored location, or arrived at a monitored location after monitoring ceased.
After pumping MW21 for 30 minutes, phloxine seemed to be present in all pumped samples
from this well at low levels. This indicates that the phloxine path was near this well, but not
close enough to be seen soon after the initial injection without more extensive pumping.
2.5 PCB Results in Spring Waters
PCB sampling was conducted at IC and Quarry B Springs. The results of those samples are
summarized in Table 4. All but one of the original PCB results reported for the IC Spring
were rejected by Viacom as biased low by the laboratory.
Some archived samples for both springs were submitted to the lab in an attempt to recover
data for the period in question. Viacom suspects that the archived sample results are biased
low because they were not properly preserved and seriously exceeded hold times. Even with
an assumed low bias, the archived sample results show that the original results reported for
all but one of the IC Spring samples were biased very low.
Viacom's investigation showed that all the biased low results were prepped in one batch by
the same analyst. This indicates an error at the prep stage. The Quarry B samples were
prepped in a separate batch by a different analyst and there is no indication that the original
reported results for Quarry B Spring are biased.
The purpose of sampling at IC Spring for PCBs during the dye test was to determine if a slug
of PCBs would arrive with the Fluorescein injected at LF6. Of the 11 samples taken at the
spring during the dye test, only the last sample result is considered valid. This one sample
result was taken on November 2 at 05:00. This was in the middle of the breakthrough curve
period for Fluorescein at the spring. The PCB result for this sample (11 ppb) is higher than
expected based on pre-remedy historic trends but not by a wide margin and is somewhat
consistent with data collected post remedy.
The purpose of collecting PCB data at the Quarry Springs was to determine if PCBs would
fall off after water was prevented from entering the swallow hole. The data does not show a
definite trend.
2.6 Conclusions for the Dye Test
Some of the Fluorescein flushed from LF6 traveled to Valhalla Cemetery in vadose
passages.
- Some of the Fluorescein did descend to the phreatic zone near well 00370.
- The Fluorescein response at IC Spring indicates there may be more than pathway
from LF6 to the spring.
- No dye was detected at Slaughterhouse Spring. This spring was sampled sporadically
for up to 1 week after injection. This indicates that this spring does not receive site
related waters quickly and is consistent with previous dye testing that showed this site
to most likely be a minor discharge area for site waters.
- There was no breakthrough curve for Fluorescein at Quarry B Spring or the weir
seep. This indicates that these springs are not carrying IC Spring underflow waters.
- Eosine appeared to travel to the east-northeast.
- Eosine was not detected at any spring. This implies either that the Fluorescein path to
IC Spring is quicker than the cosine path or that the cosine was diluted below
detection at the springs.
- Phloxine was not detected. This implies either
that the Fluorescein path to IC Spring is quicker than the phloxine path
or that the phloxine was diluted below detection at the springs.
3.0 Pump Testing
MW2 1 and MW 16 are wells on the east side of the Lemon Lane Landfill. These wells were
installed as part of the karst conduit system investigations in 2001. As part of these
investigations, these wells were pumped for extended periods of time in November 2001.
This report summarizes the data and suggests follow up investigations based on this data.
The test plan for pumping is included in Attachment 3.
During these pump tests, water was also flushed down the following wells:
LF6 twice
NN700 once
SP1 once
These water flushes were done to provide a pulse of dyes at these locations while pumping.
Dyes had previously been injected at these wells on October 31, 2001. It was suspected that
by merely flushing water at these wells, the residual dye at these locations would be flushed
into the karst system and provide additional information about the radius of influence/capture
potential of each pumping well. This report also discusses the recovery of dye at the pumping
wells and IC spring aRer each of the water flushes. The following sections discuss each test.
3.1 MW2 1 Pump Test
The pump test at this well began on November 7, 2001 at 10:00 am. The well was pumped
with a 4 inch submersible pump that was lowered to the 800 amsl elevation. The pumping
rate was set at 17 8pm and maintained for the duration of the test. The pump was shut off on
November 9 at 14:00 for a total of 52 hours of pumping. A total of approximately 65,000
gallons of water was pumped from the well. The water was treated on-site and released to
the lined retention pond in the southwest corner of the site. The retention pond outlet was
blocked so that none of the treated water could escape.
The original plan was to pump for at least three days. The pumping was halted after 52 hours
for two reasons. First, the preliminary report on the PCB samples from the pumping well and
the spring were not encouraging. Second, the post water treatment PCB levels were slightly
above the discharge limit indicating that a shutdown was necessary to correct the treatment
process.
Wells in the vicinity of the site were monitored for water level before, during and after
pumping. Flow and Conductivity at IC Spring was continuously monitored by IDEM at their
treatment facility .
In addition to sampling the well for PCBs during pumping, the well was also sampled for
dyes. This was done because of the dye injections done on October 31, 2001. It was thought
that residual levels of dyes from those injections may still be in the aquifer and the arrival
times of the dyes at the well may provide insight on the closeness of the well to the dye travel
paths. Additionally, well LF6 was flushed with 300 gallons water on November 8 at 15:30.
The injected water was water previously pumped and treated from MW2 1. Dye sampling
continued at the well to determine if water flushed on November 8 would result in a dye hit
at the pumping well.
A major goal of the pump test was to determine if PCBs at the IC Spring would be impacted.
It was hoped that eventually, high levels of PCBs would be withdrawn from the pumping
well and this would result in a substantial drop in PCBs at the spring. Samples were taken at
the spring periodically during the duration of pumping and analyzed for dye and PCBs.
The results of the MW21 pump test are summarized in Sections 3.1.1 - 3.1.6 below .
3.1.1 PCB Results at the Pumping Well
A summary of field parameters and PCB sample results for the MW21 well is shown in
Table 5. The PCBs at the pumping well started out and finish in the 5-7 ppb range. This is
not seen as a major change. Therefore, it can be concluded that the MW21 well is not on or
hydraulically well connected/near a major conduit that carries a large amount of PCBs to the
IC spring. The 5-7 ppb range compares to PCB levels at the IC spring which are typically
10-20 ppb under these flow conditions.
It is not clear why this well would produce so much less PCBs upon pumping than did
MW4I. This well is only 10 feet from 4I and the pump was placed at about the same
elevation in this well as when 4I was pumped. It was expected that it would produce a
similar level of PCBs. MW4I produced high levels of PCBs during two separate pump tests
in the summer of 2001. However, 4I was pumped for a short period of time on November 6,
2001 just prior to starting the MW21 pump test and it showed only low levels of PCBs
(1-2 ppb). It should be noted that well MW4I was modified by removing some bentonite at
the bottom of the well between the summer pump test and the mini-pump test performed on
November 6. This modification could have changed the zone that supplies most of the water
to the well upon pumping.
Because there were some PCB samples analyzed at Heritage Labs that were found to be
biased low, it is recommended that additional samples of well 4I be taken at the earliest
opportunity to determine if this well can once again produce high levels of PCBs. These
samples should be taken with some limited pumping. To determine if the hydraulics at the
well have change as a result of removing bentonite, the drawdown should be monitored
during the short pump test for comparison to the summer data.
3.1.2 Aquifer and Well Hydraulics
Table 6 provides a complete listing of the continuous monitoring well level data. The
pumping well drawdown and elevations are listed on Table 5 and shown in Figure 5.
Elevations for the other wells are shown on Figure 6. The drawdown and field conductivity
for the pumping well show that hydraulic equilibrium was achieved. The final elevation
reached at the pumping well was 814.4 feet amsl. The total drawdown for the pumping well
was 1.88 feet. This compares with over 5 feet of drawdown in well 41 when it was pumped
at a lower rate in the summer of 2001. Even though the overall aquifer conditions were drier
in the summer, this large of a difference in drawdown most likely indicates that this well is
much better connected to a water source than well 41. Well 41 is a smaller well bore than
MW21 and this smaller bore could partially explain why so much more drawdown was
achieved in MW4I. But the difference is so dramatic other factors are likely at play.
A more thorough analysis of the drawdowns for the pumping wells and monitoring wells
during both this and the MW16 pump test is included in section 3.3.
Figure 7 and Table 7 shows the flow and conductivity at IC Spring during the pump test.
The flow at IC spring dropped almost immediately upon the commencement of pumping.
While the conductivity continued a fairly normal receding limb/base flow rise. Flow also
responded almost immediately to the cessation of pumping. Conductivity appeared to
stabilize and then slightly fall the next day after pumping ended. Whether or not this is
caused by the end of pumping is confounded by a small amount of rain (.02 inches) that fell
on November 8.
The rapid response of both the spring flow and remote well levels indicates that the pumping
well is very well connected to the aquifer, and that all the wells and springs are well
interconnected. It should be noted that most of the monitored wells were drilled to at least
the same elevation as the pumping well. But one well, 4S is drilled several feet shallower,
this well also responded similar to the deeper wells. No significantly shallower or deeper
wells were monitored for water level during this pumping period to determine if they would
be similarly impacted.
3.1.3 PCBs at IC Spring
The PCB response at IC Spring to pumping at MW2 1 is shown on Table 7 and Figure 8. As
can be seen, PCBs were at about 12 ppb prior to pumping and rose to a range of 18 to 24 ppb
within 7 hours of pumping. The PCBs decreased slightly to a range of 17 to 21 ppb range
after 28 hours of pumping. The PCBs dropped to the 10 ppb range within 8 hours after the
pumping ceased. They stayed in this range for about 28 hours then rose to the 12 to 18 ppb
range.
One of the main goals of the pump test was to determine if significant levels of PCBs would
be drawn from this well while pumping and if the PCBs at the IC spring would fall during the
pumping period. This did not happen. The spring PCB levels increased during the pumping
period, drifted slightly lower while pumping and then appear to have fallen after turning the
pump off. This indicates that if there is a conduit system near MW21, it may be providing
relatively clean water to the spring.
The PCB results at the spring must be observed with some caution. It appears that some
results may be affected by the amount of time the bottle stayed in the autosampler and the
amount of heat built up in the sampler during that time. Evidence for this impact was
observed during periods of high temperatures most recently during the July/August pump
testing done at well 41. During this test period, most samples that stayed in the sampler for
more than 24 hours have lower PCB results than those that were in the sampler for less time.
For this test period, the samples from November 9 20:00 to November 11 16:00 were in the
sampler for more than 24 hours. The results for those samples may be biased low by what
appears to be in sampler volatilization losses. Therefore, the conclusion that PCBs fell at the
spring after turning the pump off on November 9 is not certain.
3.1.4 Dye Response at the Pumping Well
Dye was sampled at the pumping well to determine if any residual from the dyes previously
injected in the aquifer on October 31 would be drawn to the well while pumping. If and
when this occurred may provide an indication of how far the well is from a flow path
carrying the dyes. The dye sample results are shown on Table 8 and Figure 9.
As can be seen on the table, only a degraded rhodamine (DRWT possibly from a past
injection) was present in the well as pumping began. But within one half hour of pumping
both Fluorescein and Phloxine became detectable. All three dyes were routinely present in
all pumping samples thereafter. A large Fluorescein peak occurred at November 9 at 16:00.
This is thought to be a result of the flushing of LF6 on November 8 at 15:30.
These results along with the dye test sample results at this well suggest several things:
- This well did receive an cosine breakthrough curve during the dye test without pumping.
- This indicates it is near a path that carried cosine from the NN700 area (the southwest
corner of the site).
- This well did not have Fluorescein or Phloxine hits during the October 31 dye test but did
receive these two dyes within 30 minutes of the start of pumping the well on
November 7. This indicates that at least some portion of these dyes flowed near the well.
- The well received a hit of Fluorescein after flushing LF6 on November 8. This indicates
that at least some of the Fluorescein flushed from LF6 does get captured by this well
when pumping. However, the IC Spring also received a large hit of Fluorescein from the
November 8 flush indicating that pumping this well cannot capture all of what is flushed
from the LF6 area. Relatively speaking, the amount of Fluorescein recovered at the
spring after the flush was much larger than that recovered at this well. This indicates
there are two flow paths for waters flushed from the LF6 area and that this well is near
the smaller of the two. This further indicates that this well is not an efficient pumping
location to capture materials flushed from the epikarst at LF6. This is supported by the
low level of PCBs recovered in the well since the epikarst at LF6 has been shown to
contain high levels of PCBs.
3.1.5 Dye Response at the IC Spring
Dye samples at IC Spring were taken for some periods during the pump test period. See
Table 7 for a complete listing of the results. Only Fluorescein was reliably and consistently
detected at the spring. The analysis of the Fluorescein response to pumping at the spring is
confounded by two factors. First, the Fluorescein concentrations at the spring were receding
from the October 3l dye injection. Second, samples for dye analysis were not taken from the
period 6 hours prior to the start of pumping until about 20 hours after pumping began.
Figure l0 is a plot of Fluorescein concentrations at the spring during the MW21 pump test.
While Fluorescein concentrations during pumping are at no time higher than pre-pumping
levels, they may be higher than would be expected had the Fluorescein continued to decline
at the same rate occurring just prior to turning the pump on.
There is a large amount of dye indicated by a breakthrough curve for Fluorescein that begins
on November l 0 at 08:00 (after pumping stopped the day before). It is believed that this was
a result of the flushing of water at LF6 that occurred on November 8 at l 5:30. Note that
there is only a single peak to this curve.
3.l.6 Conclusions and Recommendations for the MW2l Test
Pumping MW2 l did not lower the PCBs at IC Spring after 52 hours. It also appears that
pumping this well will not capture most of the materials that are flushed from the epikarst
near LF6.
Hydraulic indicators such as low flow water levels and quick equilibration during pumping
(along with relatively low drawdown per gallon/minute pumped) show that this well is near
or on a major conduit. This conduit most likely drains the 795-800 elevation zone around the
site and possibly all zones in the northern portion of the site.
These results along with the previous dye test indicate that there are at least two major flow
networks feeding the spring from the site area. It appears that most of the PCBs released
from the southern epikarst region do not use the flow network associated with this well to
reach the spring. These results along with the previous dye testing suggest that either:
- The flow network carrying the PCBs from the southern epikarst is at a different
elevation. This is because all the wells around the site that were monitored at the
pumping well elevation responded in a manner which indicates they were connected
to the pumping well.
- Or the flow network is at a similar elevation, but much of the transport occurs in the
epikarst and the connection between zones occurs so far from the pumping well that it
was not affected by pumping this location.
It is not clear what happened to the high PCB levels previously found in well 4I. This well
should be resampled to determine if the previous high levels were just a random flush of a
small pocket rather than a long term issue.
3.2 MW16 Pump Test
The pump test at this well began at November 13, 2001 at 12:00. The well was pumped with
a 4 inch submersible pump that was lowered to the 800 amsl elevation. The pumping rate
was set at about 17 8pm and maintained for the duration of the test. The pump was shut off
on November 19 at 08:30 after a total of 140 hours. A total of approximately 143,000
gallons of water was pumped from the well. The water was treated on-site and released to
the lined retention pond in the southwest corner of the site. The retention pond outlet was
blocked so that none of the treated water could escape.
The test was continued for significantly more than three days because the MW2 1 test was cut
short and it was desired to make sure that adequate time was allowed for full hydraulic and
chemical equilibrium to be established.
Wells in the vicinity of the site were monitored for water level before, during and after
pumping. Flow and Conductivity at IC Spring was continuously monitored by IDEM at their
treatment facility.
In addition to sampling the well for PCBs during pumping, the well was also sampled for
dyes. This was done because of the dye injections done on October 31, 2001. It was thought
that residual levels of dyes from those injections may still be in the aquifer and the arrival
times of the dyes at the well may provide insight on the closeness of the well to the dye travel
paths. Additionally, well LF6 was flushed with 300 gallons water on November 16 at 15:30.
This water was well water that had been processed thru the treatment trailer. Dye sampling
continued at the well to determine if water flushed on November 16 would result in a dye hit
at the well.
A major goal of the pump test was to determine if PCBs at the IC Spring would be impacted.
It was hoped that eventually, high levels of PCBs would be withdrawn from the pumping
well and this would result in a substantial drop in PCBs at the spring. Samples were taken at
the spring hourly or every 4 hours during the duration of pumping and analyzed for dye and
PCBs.
The results ofthe MW16 pump test are summarized in sections 3.2.1-3.2.6.
3.2.1 PCB Results at the Pumping Well
A summary of field parameters and PCB sample results for the pumping well is shown in
Table 9. The PCBs at the pumping well started out at about 8 ppb and slowly declined to a
minimum of .6 ppb and then stabilized in the 2.5-3 ppb range. These results are generally
consistent with the short term pump test conducted in the spring of 2001 at this well.
It can be concluded that the MW16 well is not on or hydraulically well connected near a
major conduit that carries a large amount of PCBs to the IC spring. The 2-3 ppb range
compares to the 5-7 ppb range withdrawn from MW21 while pumping and with PCB levels
at the IC spring which are typically 10-20 ppb under these flow conditions. Based on these
results, this well is not as well positioned as MW21 for PCB recovery.
3.2.2 Aquifer and Well Hydraulics
The pumping well drawdown and elevations are shown in Figure 11 and Table 9. Elevations
for the other monitored wells are shown on Figure 12 and Table 10. The drawdown and field
conductivity for the pumping well show that hydraulic equilibrium was achieved. Note that
the apparent large decline in conductivities at 16:00 on November 15 is believed to be an
instrument problem. All conductivities after this time are considered biased low.
The final elevation reached at the pumping well was 814.38 feet amsl. The total maximum
drawdown for the pumping well was 1.94 feet. This compares with over 5 feet of drawdown
in well 41 when it was pumped at a lower rate in the summer of 2001 and with 1.88 feet seen
when pumping MW21. Even though the overall aquifer conditions were drier in the summer,
this large of a difference in drawdown most likely indicates that this well is much better
connected to a water source than well 4I and similarly connected to the aquifer as MW21.
A more thorough analysis of the drawdowns for the pumping wells and monitoring wells
during both this and the MW21 pump test is included in section 3.3.
Figure 13 shows the flow and conductivity at IC Spring during the pump test. The flow at IC
spring dropped almost immediately upon the commencement of pumping. While the
conductivity continued a fairly normal receding limb/base flow rise. Flow also responded
almost immediately at the cessation of pumping. Conductivity appeared to stabilize and then
fall the next day after pumping ended. This is the same trend as seen at the end of the MW21
pump test. The interpretation of a conductivity fall the day after pumping ceased is
somewhat confounded by a small rain event that occurred on November 19 (about .2 inches
of rain fell between 07:00 and 13:45).
The rapid response of both the spring flow and remote well levels indicates that the pumping
well is very well connected to the aquifer, and that all the monitored wells and IC Spring are
well interconnected. It should be noted that most of the monitored wells were drilled to at
least the same elevation as the pumping well. But one well, 4S is drilled several feet
shallower, this well also responded similar to the deeper wells. No significantly shallower or
deeper wells were monitored for water level during this pumping period to determine if they
would be similarly impacted.
3.2.3 PCBs at IC Spring
The PCB response at IC Spring while pumping at MW16 is shown on Table 11 and
Figure 14. As can be seen, PCBs were in the 12-14 ppb range prior to pumping and rose to
about 20 ppb within 5 hours of pumping. The PCBs remained at these higher levels until
about 26 hours after pumping began when they dropped to the 7-1 1 ppb range for about
90 hours. PCBs then rose back to the 10-16 ppb range. After 72 hours of pumping the PCBs
again dropped to the 10 ppb level for approximately 16 hours and then they fluctuated
between 10 and 16 ppb for the next 24 hours before rising back to the 1~20 ppb range for
the final twelve hours of pumping.
It is not clear why there would be so much apparent cycling of PCB levels during this test.
There was no significant rainfall during the test and hydraulic parameters at the pumping
well and observation wells appeared stable. The only perturbations introduced to the system
was a series of three water flushes. The first flush occurred in SPI on November 14 at 15:30.
The second occurred on November 15 at 1 1:30 at NN700 and the third occurred on
November 16 at 15:30 at LF6. The NN700 flush was 100 gallons while each of the others
was comprised of 300 gallons of treated well water. It is believed that these flushes of clean
water were too small to explain the relatively large changes in PCB levels that appear to have
occurred.
The PCB lab reports were reviewed to determine if lab variance or errors could account for
these cycles. There was no obvious lab errors found that could account for the observed
changes. However, as noted in the MW2 I test report, it is possible that the length of time
that any particular sample sat in the autosampler could have influenced the result. As in that
test, samples that sat in the sampler for longer periods of time tend to have lower levels of
PCBs. This could explain the apparent cycling levels of PCBs.
One of the main goals of the pump test was to determine if significant levels of PCBs would
be drawn from this well while pumping and if the PCBs at the IC spring would fall during the
pumping period. While there are some unexplained drops of PCB levels at IC Spring during
the pumping period, these drops are not consistent or large enough to consider them a direct
benefit of pumping at this well. Additionally the level of PCBs withdrawn from the well
dropped as pumping began and stabilized at a low level that would not indicate a significant
impact on PCBs at the spring would be expected.
3.2.4 Dye Response at the Pumping Well
Dye was sampled at the pumping well to determine if any residual from the dyes previously
injected in the aquifer on October 31 would be drawn to the well while pumping. If and
when this occurred, may provide an indication of how far the well is from a flow path
carrying the dyes. The dye sample results are shown on Table 12.
As can be seen on the table, at the very beginning of pumping there were no significant levels
of any of the recently injected dyes. After 8 hours of pumping Fluorescein begins to show up
at low levels. These levels build a breakthrough curve with a peak 28 hours after pumping
began. The magnitude of the Fluorescein levels are low relative to those recovered at MW'I
or IC Spring. Speculation is that this Fluorescein is coming from a continual slow release of
dye from the LF6 conduit. This slow release hits the part of the phreatic zone influenced by
this pumping well at some location, the travel time to the well of 8-28 hours may be
indicative of the distance to that location. Figure 15 shows the Fluorescein results at this
well.
Sporadic hits of cosine are also periodically seen after 8 hours of pumping. Curiously, there
is not a breakthrough curve for cosine after the NN700 well is flushed on November 15 at
11:30. However, the cosine is more consistently present for the next 20 hours after the flush.
No phloxine is detected in the well even after SPI was flushed on November 14.
A second low level breakthrough curve for Fluorescein is seen starting 8 hours after LF6 is
flushed on November 16. This indicates that at least some of the Fluorescein flushed is
captured by this well.
These results indicate the following:
- Phloxine does not take a path from SP I to the IC Spring which is influenced by this
well.
- The cosine pathway is somewhat influenced by this well but not to a significant
extent.
- Minor portions of the Fluorescein pathway can be influenced by this well.
Overall, these results indicate this location is less efficient than MW2 I for capture of site
area waters and PCBs.
3.2.5 Dye Response at the IC Spring
Dye samples at IC Spring were taken throughout the MW16 pumping period. See Table 11
for a complete listing of the results. Only Fluorescein was reliably and consistently detected
at the spring. These results are also shown on Figure 16.
The analysis of the Fluorescein response to pumping at the spring is confounded by the fact
that the Fluorescein concentrations at the spring were receding from the October 31 dye
injection and again from the November 8 flushing of LF6.
As can be seen from Figure 16, Fluorescein concentrations during pumping are slightly
higher for the first day then they were immediately prior to the start of pumping. They then
continue a typical receding limb decline with a couple of perturbations until the large
breakthrough response on November 19. The breakthrough curve starting at 12:00 on
November 19 is attributed to the flushing at LF6 that occurred on November 16 at 15:30.
This is a travel time of about 68 hours. With flows at IC Spring between 30 and 40 8pm
during this time period, an expected travel time of 50 to 65 hours was expected. This is fairly
good agreement considering LF6 is an epikarst location.
Comparing the size of the breakthrough curve at the spring to the breakthrough at MW16
from the November 16 flush shows that by far most of the Fluorescein flushed at LF6 was
not captured at the pumping well. Also note that the Fluorescein response at IC Spring on
November 19 is a two peak response. This compares with the original Fluorescein response
from the October 31 dye injection. Recall that the Fluorescein response from the November
8 flush (while pumping MW21) was a single peak at this spring.
Table 13 shows a summary comparison of dye results obtained for each of the Fluorescein
recoveries resulting from the October 31, November 7 and November 16 flushes.
3.2.6 Conclusions and Recommendations for MW16 Test
It appears that pumping MW16 cannot significantly lower the PCBs at IC Spring. It also
appears that pumping this well will not capture most of the materials that are flushed from
the epikarst near LF6.
Hydraulic indicators such as low flow water levels, quick equilibration and dye recovery
during pumping (along with relatively low drawdown per gallon/minute pumped) show that
this well is well connected to a major conduit but not as close to the conduit as MW21. The
conduit affected most likely drains the 795-800 elevation zone from the southern portion of
the site.
3.3 Analysis of Drawdown Data for MW21 and MW16 Pump Tests
Data Collected
The following wells had hourly water levels recorded by dataloggers for both pump tests:
MW15
MW17
MW6
NN625
MS1
MW8s
SP1
In addition, hand measured water levels were taken in the pumping wells and in the
observation wells mentioned above and in the following other observation wells:
MW19
MW18
MW20
MW41
MW4s
MW2
NN700
00587
00387
00370
00300
NN300
00125
NN12
NN300A
Table 5 shows the data taken for MW21 while it was the pumping well, and Table 9 the data
for MW16 while it was the pumping well. Table 14 shows the data for the spot observations
measured by hand.
Method of Analysis
There are two ways of looking at the drawdown data from the pump tests. One is to perform
time-drawdown analysis and the other is to perform distance-drawdown analysis.
Time-drawdown analysis is based on the Jacob Assumption for the Theis Non-equilibrium
theory. This is the analysis of the observation wells during pumping as the levels are
declining before they reach maximum drawdown or equilibrium. The Theis theory assumes:
- The transmissivity of the aquifer tapped by the pumping well is constant during the
test to the limits of the cone of depression.
- The water withdrawn from the aquifer is derived entirely from storage and is
discharged instantaneously with the decline in head.
- The discharge well penetrates the entire thickness of the aquifer, and well bore
storage is negligible.
The Jacob Assumption is that the data in a semi-log graph of drawdown vs. time (with
drawdown on the linear axis and time on the logarithmic axis) will plot as a straight line,
once stead-shape conditions have occurred in the cone of depression. This means that the
slope of the line is proportional to the pumping rate and the transmissivity of the aquifer.
Departures of the data plot from a straight line may give information about changes in
aquifer properties or proximity to boundary conditions.
Distance-drawdown analysis makes the same assumptions as the Theis theory. Comparisons
can be made during pumping if measurements are made simultaneously. If withdrawals have
occurred long enough that increases in recharge andJor decreases in discharge have balanced
to the rate of withdrawal and drawdown has ceased, then cone of depression in said to be in a
steady state. Resumption of drawdown or recovery of levels, if pumping rate remains
constant, reflect the intersection of the cone with boundary conditions. Again, the Jacob
Assumption is that the data in a semi-log graph of drawdown vs. distance from the pumping
well (with drawdown on the linear axis and distance on the logarithmic axis) will plot as a
straight line. The slope of the line is proportional to the pumping rate and the transmissivity
of the aquifer. Departures of the data plot from a straight line may give information about
changes in aquifer properties or proximity to boundary conditions.
Pump Test Analysis
Figure 17 is a semi-log of drawdown vs. time for the MW21 pump test and Figure 18 is the
plot for the MW 16 test. In the MW21 test, drawdown levels off at 23-25 hours, and then
begins again at a higher rate. If this was not an increase in pumping rate (and field notes do
not indicate any increase) then the cone of depression reached a less transmissive part of the
aquifer. Because this happens nearly simultaneously in all observation wells, we might
speculate that the upstream end of the branchwork system of conduits had been reached.
Drawdown then appears to reach steady state at 36 hours. The recovery at 49 hours probably
indicates a decrease in pumping rate.
In the MW16 test the pumping rate was slightly less (16.8 vs. 17.0 8pm) and the wells appear
to begin to reach equilibrium at 21 hours. At 27.5 hours, 47.5 hours, and 76 hours water was
flushed into wells NN700, SPI, and LF6-8 respectively, during the MW16 test. The water
flushes into the phreatic wells (NN700 and SP I ) seems to have caused an instantaneous rise
in water levels in all wells. The water flushes into LF6-8 during the MW16 and MW21 tests
does not seem to have had much of a discernable effect. A very small rise in NN300A on
November 16 at 16:30 may have been due to the LF6-8 flush, but it is too small to be
definite. The effect of a mere 100 and 300-gallon flush indicates the aquifer has very small
storage capacity. In the MW 16 test, as in the MW21 test, drawdown continues after the 21-
hour hiatus, perhaps indicating a discharge boundary has been passed. Drawdown then
appears to reach steady state at about 83 hours. There is a slight recovery at 94 hours, again
which may be due to a decrease in pumping, and then steady state is achieved again at 105-
106 hours, albeit at a slightly higher level.
The slopes of the lines on Figure 17 and 18 are all remarkably parallel. This indicates that
the zone being pumped has a relatively homogeneous transmissivity. However, there appears
to be a greater degree of drawdown from MW 16, despite the nearly equal pumping rates.
This can be seen in Figure 19, which compares drawdown from observation wells similar
distances from their respective pumping wells, and Figure 20, that compares drawdown in
MW8s, nearly equidistant from both pumping wells. Figure 21 shows the drawdown in the
pumping wells. Until about 240 minutes (4 hours) MW16 is drawing from a less
transmissive zone than MW21. Our interpretation is that MW16 is drawing water more from
the anastomotic zone at the 795' to 800' elevation, while MW21 is drawing water from a
nearby larger conduit. That is why pumping from MW16 draws the anastomotic zone down
almost 50% more than MW21.
Figure 22 is the plot of maximum drawdown vs. distance for the MW21 test and Figure 23 is
the plot of maximum drawdown vs. distance for the MW16 test. For the MW21 test, SP I
and MW8s appear to show less drawdown than would be expected. For the MW 16 test
MW 17 does not seem to show the same relative drawdown as well as SP 1 and MW8s.
Figure 24 is a plot of all phreatic wells measured on November 16 (between 70 and 73 hours)
during the MW16 test. That plot shows particularly large deflections from the straight line
plot of data for the 4-series wells (20, 4I, 21, 4s). This phenomenon is manifested on
Figure 18 in the order of relative drawdown. The closed well to MW16 (with datalogger)
was MW 15, which has the largest degree of drawdown, the next closed well is MW17, but
MW6, NN625, and MS 1 have greater degrees of drawdown.
So the hydraulic data is showing that the anastomotic zone in the 795-800' elevation is
widespread and relatively uniformly dissolutioned. However, there is another network of
conduits, which, while still in connection with this anastomotic zone, are not well connected
with each other. On Figure 22 MW7 appears to show expected drawdown levels when
MW21 is pumping. But on Figure 23, MW17 appears as an anomaly when MW16 is the
pumping well. This indicates that MW17 is on, or closer to, a different network of conduits
than MW16. Based on Figure 24, our interpretation is that the 4-series wells are near a major
branch conduit. It should be noted that the 4-series wells are the potentiometric low point in
base flow periods, and that the low flow order is the same as the deflection in Figure 24 i.e.
MW20 > MW4I > MW21 > MW4s.
4.0 Sargent's Pond Injection Test
The Sargent's Pond injection test consisted of releasing the water stored in the lined retention
pond to Sargent's Pond. This water came from the previous pump test (after treatment for
removal of PCBs). There was approximately 200,000 gallons of water stored from the pump
tests. The goal of the test was to see how the water once released would impact the pond
level, well levels around the site and flow/PCBs at IC Spring.
Prior to release, continuous well level monitors were installed at both phreatic and shallow
wells/piezometers near the site. Also an autosarnpler was set to take PCB samples at IC
Spring. The following locations were continuously monitored:
NN300A, SP1, PZD, PZBD, B3, MW6, MW15, MW17, NN625, MS1, Sargents Pond Level
and IC Spring flow/conductivity
The release occurred on November 20, 2001 at 13:30. The phreatic well levels are shown on
Tables 15 and 16. The shallower well and Sargent's Pond data are shown on Table 17. IC
Spring data is shown in Table 18.
Refer to Figure 25 for a view of the phreatic well data. Figure 26 shows the shallower well
and Sargent's Pond data and Figure 27 the spring data.
The most obvious result of this testing is that there was not a large impact on well levels or
spring flow. This is confimned by the rise and then negligible fall in Sargent's Pond level
after the release. This shows that the pond has a low leak rate in this level range.
The flow records at the IC Spring show what a small rise in flow occurs after release of the
water to the pond. The rise is approximately 4-5 8pm.
The PCBs at IC Spring were sampled every two hours until November 23 10:00. Refer to
Figure 28. There is a large apparent drop in PCBs beginning on November 21 at 12:00.
While this could be do to dilution water added to the aquifer from the injection, it is more
likely an artifact of sampling. Again, the samples taken on November 21 from 12:00 on
spent more than 24 hours in the autosampler and are most likely biased low. The results of
November 23 which spent little time in the sampler are most likely liKle influenced by
sampling artifacts. These show a lowering of PCBs also from pre-injection levels.
5.0 Overall Conclusions (Note this includes all tests)
The overall conclusions from these tests indicate the following:
ù Material flushed from LF6 appears to take two pathways from the site to the spring.
ù It appears that pumping MW21 was much more successful than MW16 at
intercepting the lesser of these two pathways.
- One major pathway from LF6 is into Valhalla Cemetery while still in the epikarst.
Some of the epikarst waters descend to the phreatic zone near well 00370.
- Wells on the east side of the landfill at the tested depth are not effective at
intercepting flushed PCBs from the epikarst.
- The dye results suggest that capturing PCBs as they are flushed may be most
effectively done either in Valhalla Cemetery, or at the extreme southern portion of the
landfill up against the railroad tracks.
- These results also suggest that dewatering the epikarst may be effective at lowering
both non-storm flow and storm pulse PCBs to the spring.
- Most of the materials leaving the southeast corner of the site in the epikarst must be
descending to a portion of the phreatic zone that was not impacted by either pump
test. Additional investigations are necessary if these zones are to be found.
- Some of the PCB results at IC Spring are questionable because the samples sat in the
sampler for longer periods of time. This is most likely caused by volatilization of
PCBs from the uncapped bottles as the sampler warmed up in the sun. The weather
was unusually warm during November testing. Future testing should take precautions
against this sort of potential error such as icing the sampler and minimizing the time
that a sample remains in the sampler to less than 24 hours.
- Sargent's Pond has a low leakage rate for elevations up to 843 feet arnsl.
Footnotes
1Palmer Arthur N., "A Statistical Evaluation of the Structure Influence on Solution Conduit Patterns", Karst
Modeling, Karst Waters Institute Special Publication 5 1999.
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